A
description of bringing an idea from first concept to a marketable item
A few years ago when I was a Project
Engineer at Honeywell Security Systems and Custom Electronics, I was
asked to help the purchasing department solve a problem that they had
procuring an electromechanical component. The component was a switch,
composed of a special alloy. The special alloy allowed the switch
to open when the temperature was lower than 42°F, with a high degree of
accuracy and low hysteresis; which means that when the temperature
became warmer than 42°F, that it would close again.
The price on the switch kept increasing
and the manufacturer had difficulty producing the item. This was due to
the alloy supplier no longer being able to make a properly constituted
alloy. The switch manufacturer elected to close the factory where the
switch was being made. I glibly said that I could do the switch using
solid state components for a less expensive total material price.
I developed a design and sold the
Marketing Department on the idea. In addition to sensing the occurrence
of low temperature, I suggested also sensing warm and hot temperatures
as possible environmental alarm conditions. Marketing liked the idea and
asked me if I could sense the temperature in a refrigerator or freezer.
I explained that I could, if I used a remote thermistor probe. In
addition, I suggested that I also could sense the presence of a flood
condition with a different type of sensing probe.
I chose to use a microcomputer (MCU) as
the basis for the measurement and as a mechanism for formulating a
serial digital message that would be sent out over a radio transmitter link.
This was done
periodically from this sensor for ‘housekeeping’ functions, such as
indication that a good battery condition exists and that the unit is
working and a special message would be sent if there was a temperature
or water alert. The MCU that I chose was capable of making a temperature
measurement The MCU only measured temperature with an accuracy of ±10°F,
which was not good enough. This inaccuracy was caused by an offset error
variation from unit to unit. To obviate the effects of that offset, I developed a
technique of calibration during the loading of the program code. The way
that it worked was that after the program was loaded, a subroutine would
execute that would measure a ‘control’ thermistor and estimate the
ambient temperature. This measurement was ratiometric and was
extremely accurate. Then I measured the temperature using the MCU and
calculated the difference. Using an equation in the MCU that simulated a
piecewise approximation of the thermistor curve, I was able to develop
a correction factor that ensured that the adjusted MCU measurement was
accurate within ±2.5°F. When this product is used with an external
thermistor, the specified accuracy improves to ±1.0°F. If the product was calibrated
with a paired thermistor, considerably improved accuracy, better than
the ±1.°F accuracy could be obtained. At this point, for better than the
1 degree accuracy, manufacturing facilities would have to be modified to
ensure that the test and storage areas of the pre-test product are
stabilized.
This product was capable of being used
for six different functions versus the older product with the
electromechanical switch which was only usable for one function. The price
of the Bill of Materials (BOM) for my re-designed product was only 33%
of the price the original product's BOM. This resulted in a definite
win-win situation. This product is called the Honeywell 5821.
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